WEEK 2: 01/19/24
We tested photoelectric sensors to see which sensors are the most effective for the intake and the shooter of the robot.
WEEK 2: 01/20/24
We started planning and wiring the electrical board. We reused wire from other robots, so they are not all the perfect length. In the future, we will cut wire according to the specific components on the robot, so that we will not have excess wire.
WEEK 2: 01/21/24
Today we began wiring components onto the electrical board. We also tested the SPARKMAXs removed from the Rapid React robot. Then we confirmed that the CAN wiring is correct.